Page 1 of 2 12 LastLast
Results 1 to 10 of 12

Thread: Z axis stall

  1. #1

    Default Z axis stall

    Hi all, fairly new to Carvewright and not sure of all the technical terms yet.

    I was was carving a project overnight and when I got up the next morning it was stopped but not completed. It had an error message and the bit (still in z truck) was about 3 inches from the last correctly carved portion of the piece. The bit was all the way down stuck in the wood and making a terrible high pitch sound. I didn't have a chance to fix it then is I just turned the machine off and went to work. I did some research, stumbled across this forum and read some of the other suggestions. I cleaned it up and it looked like it was brand new (inside too). Tried a practice piece. Before it could start a practice project I noticed the bit was all the way down, like below the red belts, and it was making the awful high pitch noise again. Called customer service and said to go ahead and change to carve tight spindle. I did that this afternoon and the problem is still happening. Please help!?!? Keep in mind I don't understand a lot of the technical terms.
    Thanks!

  2. #2
    Join Date
    Aug 2008
    Location
    The Great Texas Gulf Coast
    Posts
    5,314

    Default

    Scares me to death, when people tell stories that include "when I got up" or "when I got back"...

    Glad it hadn't caused a fire.
    CarveWright CX Packaged System - starting at $2000
    CarversClub 1 Year Subscription - $150.00/year
    Adv. Support w/out CC membership - $25.00/issue
    CarveWright Community Forum - PRICELESS!

  3. #3
    Join Date
    Nov 2008
    Location
    Vancouver Island
    Posts
    8,193

    Default

    Welcome to the forum. It is hard to understand what actually happened from your post. You need to run through a simple project and carefully watch what happens. (Keep a finger on the stop button.)

    Other info would also help. Machine model. How many hours.

    The behavior could be software. It cannot hurt to format and reflash the card before you try again.

  4. #4

    Default

    Quote Originally Posted by lynnfrwd View Post
    Scares me to death, when people tell stories that include "when I got up" or "when I got back"...

    Glad it hadn't caused a fire.
    Thanks for your "help".

  5. #5
    Join Date
    Jan 2007
    Location
    NE PA USA
    Posts
    9,984

    Default

    First things first... WELCOME.....

    Second thing.... Please re consider leaving your machine run un attended.... It can malfunction and catch on FIRE.... not a good thing... I run my machine in the wood shop next to my Laser Shop where I am now, BUT... I listen on a wireless intercom, WATCH on a wireless Video Camera Monitor, and have a SMOKE detector above the machine...

    Many years ago I was running my machine and was 10 feet away on my deck and I hear my Smoke Detector turn on... I turn and my FLEX was Smoking and just catching on FIRE....

    OK... The Problem... Since you had to change to a Carve Tite Chuck then the machine is likely a older unit.... The "A" Series serial numbers like all 4 of my machines had a problem in the early years with a 18 pin FSC Cable, the flat cable to the Z Truck. The fine wires would snap... OR the early Z Encoders in the Servo Motor would fail and the machine would DRILL DOWN INTO THE BOARD.... and Stall.... could catch on FIRE TOO.....

    The FIX.... does your machine have the A907 Upgrade? See Pictures.... Upgrade has the WINGS on the Circuit Board to hold the big plug.

    And you cannot MIX and MATCH the old 18 pin and new 14 pin parts.... ALL MUST BE 14 pin.... OR the machine can short out.... So Circuit Board on the Z Motor, Flat 14 pin Cable, and Other end Circuit Board with WINGS....

    AND Replace the Z Motor.... That is where I would start....

    See Pictures.... I call the old version a 16 pin in the picture but it was 18 pin.... A Senior Moment.... The 14 Pin THICKER wire work GREAT and end many problems.

    Good Luck,

    AL
    Attached Thumbnails Attached Thumbnails DSC06680_WEB.jpg   DSC06680a_WEB.jpg   DSC06545_WEB.jpg   DSC06680a_WEB.jpg  

    DSC06659_WEB.jpg   DSC06656_WEB.jpg   DSC06655_WEB.jpg  
    Last edited by Digitalwoodshop; 06-10-2016 at 03:51 PM.
    Favorite Saying.... "It's ALL About the Brass Roller"..... And "Use MASKING TAPE" for board skipping in the X or breaking bits.

    Follow ME on Facebook http://www.facebook.com/pages/Accoun...50019051727074

    www.PoconoDigitalWoodshop.com

    www.AccountabilityTag.com


  6. #6

    Default

    Mine does that. I found that my cover switch on the right side top keeps tripping. I push the cover down hard and it will restart. I now tape it down tight. It still shut down so I put a small piece of wood between the cover tit and the switch. I know, pretty lousy rig for a 2500 dollar machine, but I can't find any information on how to adjust it.

  7. #7
    Join Date
    Sep 2007
    Location
    Northern Colorado
    Posts
    7,962

    Default

    The hinges for the clear cover or the switch screw might have slipped or are loose. Try adjusting them.
    RingNeckBlues
    My patterns on the Depot
    DC-INSERT It Just Sucks!

    Proven to out perform all others!
    Buy CarveWright
    Colorado FaceBook Users Group


    All patterns and projects that I share on the CarveWright forum are for your personal carving purpose. They are not to be shared, sold or posted on any other web site without permission from RingNeckBlues Designs.

  8. #8
    Join Date
    Jan 2007
    Location
    NE PA USA
    Posts
    9,984

    Default

    BETTER to use the "Seat Belt" trick... Install a piece of tape like the picture shown with the cover up 1/4 so when down it holds the cover tight to the switch. I did my fix on the left switch but your machine needs the fix on right side.
    Attached Thumbnails Attached Thumbnails DSC02537_WEB.jpg  
    Favorite Saying.... "It's ALL About the Brass Roller"..... And "Use MASKING TAPE" for board skipping in the X or breaking bits.

    Follow ME on Facebook http://www.facebook.com/pages/Accoun...50019051727074

    www.PoconoDigitalWoodshop.com

    www.AccountabilityTag.com


  9. #9

    Default

    UPDATE…kinda
    Machine still malfunctioning. Here’s more info on the problem:
    Problem: Z Axis stall EO6-0313
    Machine makes really loud high pitch sounds as soon as it’s powered on. Z axis stall error as soon as I initiate a project. ALWAYS happens on the far side away from keypad.
    Here’s more info about the machine:
    B series
    Dad bought it 7 or 8 years ago (total guesstimate). He never learned how to use the software so it’s just been sitting. He decided to sell it but I commandeered it about 6 weeks ago.
    Total cut motor time: 28 hours, 36 minutes
    Carvetight spindle
    Here’s what I’ve done to attempt to fix the problem:
    1. Called customer service- they said change to carve tight spindle. Bought and did that. Problem still occurred
    2. Called customer service- they said it was the Z motor. Bought and changed that. Problem still occurred.
    3. Called customer service- he sent me some documents on:
    a. Z axis stall
    b. Y axis stall (thought I’ve never had a Y axis stall)
    c. Random X,Y,Z axis stalls (though I’ve never had an X axis stall either)
    4. Following prompts on Z axis stall document (here’s more info on the problem/machine)
    a. B series model
    b. Machine not run on same circuit or a long cord
    c. Only Z stall has occurred thus far
    d. Machine does not power off after Z stall
    e. Z truck is able to be moved by hand when powered OFF
    f. It does not move roughly when powered OFF
    g. The Z truck is MUCH harder to move when powered on.
    h. The Z truck sensor check numbers do not change when the machine is moved up and down by hand
    i. The Y truck sensor check numbers do not change when the machine is moved by hand
    j. The board tracking sensor numbers DO change when moved


    The ribbon cable is in very good shape. I really need to figure out what’s wrong. I’ve had a few people want to purchase carvings from me but I can’t do them and I can’t afford to keep buying parts that aren’t fixing my issue. Any other suggestions??

  10. #10
    Join Date
    Nov 2010
    Location
    Heber Springs, Arkansas
    Posts
    42

    Default

    I had this same issue and after lots of trouble shooting all I needed to do was take the back cover off of my Z Motor and clean it out and put it back together to fix.

Page 1 of 2 12 LastLast

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •